Paper The following article is Open access

Aerodynamic Investigation of Propulsion Integration for a Low Noise Hybrid Wing-Body with Podded UHBR Turbofan Engines

Published under licence by IOP Publishing Ltd
, , Citation Dennis Keller 2024 J. Phys.: Conf. Ser. 2716 012008 DOI 10.1088/1742-6596/2716/1/012008

1742-6596/2716/1/012008

Abstract

The presented work examines the aerodynamic challenges of podded ultra high-bypass engines installed on a short/mid range low noise hybrid wing body configuration. After assessing the initial engine integration design, sensitivity studies regarding the impact of the freestream Mach number, engine position, and the engine incidence angle on the interference drag are discussed. Then, shape modifications of the nacelle and the center-body based on 2D RANS optimizations are presented. The results indicate that in order to reduce the initially massive interference drag, the overall aircraft design either has to allow for a modified engine position or for reshaping of the center-body's upper surface. With the latter, an overall drag reduction of –44 % was achieved.

Export citation and abstract BibTeX RIS

Content from this work may be used under the terms of the Creative Commons Attribution 3.0 licence. Any further distribution of this work must maintain attribution to the author(s) and the title of the work, journal citation and DOI.

Please wait… references are loading.
10.1088/1742-6596/2716/1/012008